Well, I completed the adjustment on the transmission cable this weekend. After initially lengthening the cable - getting back 5th, but losing Reverse, first and second - I shortened it 1/4 turn until I had everything, so life is now good. I took the car out driving and put about 100 miles on it and it shifts very smoothly. I am still having problems with a high idle. I tested the frequency valve and it is good. The car was idling warm around 2000 RPM's, and I started to mess with the plug that goes to the idle speed motor and the RPM's suddenly dropped down to a steady 900 RPM's... I thought great, the connections are dirty, easy fix! So I cleaned up the connections, plugged it back in and I was back at 2000 RPM's, and no amount of playing with the plug would change anything. After taking the car out for a spin, it was then idling at 3000 RPMs. I am pretty sure the mixture is off because the exhaust smells bad, and it is sucking gas at an unreal rate. I tried adjusting the mixture screw because I am sure it had already been tampered with but couldn't get the mixture screw to budge... I snapped my hex key trying. Now I need to figure out how to get the head of the hex key out of there. >From what I've given, does anyone have any suggestions on how to diagnose this? I'm confused as to why that mixture screw won't move either. Thanks in advance.. Mike Polzin To address comments privately to the moderating team, please address: moderators@xxxxxxxxxxx For more info on the list, tech articles, cars for sale see www.dmcnews.com To search the archives or view files, log in at http://groups.yahoo.com/group/dmcnews Yahoo! Groups Links <*> To visit your group on the web, go to: http://groups.yahoo.com/group/dmcnews/ <*> To unsubscribe from this group, send an email to: dmcnews-unsubscribe@xxxxxxxxxxxxxxx <*> Your use of Yahoo! Groups is subject to: http://docs.yahoo.com/info/terms/